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Yes, you read that title correctly. After many months of effort, this homemade-from-scratch electric steam boiler is finally going to make steam. Before we’re done, we’ll learn some sobering lessons about the dangers of live steam.
Now that our boiler is pressure-tested and all the accessories are hooked up, we’re ready to add heat to water and cause some trouble. Unlike a traditional fired boiler which would use fuel pellets, coal, wood, or some other combustible, this crazy contraption is “fired” with an electric immersion heating element built into the structure. In order to test making steam, we need to rig up the electrical bits.
One of the things they used to drill into engineers in school is that you should always take notes on your work. This is such a foundation of engineering education that “engineer notebooks” are a specific genre of prepackaged dead trees. The reason for this is that generations of engineers have learned the hard way that you won’t remember all the things you think you will. I was taught this, I knew this, I’ve been burned by this before, and yet…. I ignored it.
You may recall that way back in the very first post in this series, I rigged up a contactor with my heating element and thermoswitch. I did this make sure the whole crazy system would work, and also to learn how to use a contactor, since I had never done so before. The end result was pretty simple wiring-wise, so I didn’t bother writing it down, confident I would remember how it was done. I suppose I never imagined it would take me seven months to get back to the point where I needed wiring again, but here we are.
What I ended up doing was studying the photos from my own original blog post, trying to deduce how it was hooked up. Unfortunately, the camera angles were not great for this purpose.

This was the best photo I had of the original setup, but the connections around the wire nuts were maddeningly obscured.
Between the photos and my own long history in electronics, I felt I could deduce how to wire up this contactor. Before risking my expensive (and now difficult-to-remove) heating element, I wired up the contactor and thermoswitch, but substituted my multimeter for the heating element. My reasoning was that if I can get to a point where the thermoswitch toggles on and off at a particular temperature, causing 120V or 0V to appear on the big end of the contactor, I’ll have success.
After hooking everything up, I couldn’t get the desired result. No matter what, the contactor always showed 120V on the output. Strangely, the contactor has an LED on it indicating when the big end is energized, and the LED would go on and off as expected as the thermoswitch changed temperature. It seemed very much like the contactor simply wasn’t working properly. Even when “off”, it was showing 120V on the output. It seemed impossible that the contactor was bad, since it was known to be working before, and had done nothing but sit in a box on the shelf for six months.

Using my multimeter as a proxy, I tested the electrical setup. However, I couldn’t get it to work like I had before!
This is an interesting example of where your own knowledge and experience can sometimes lead you astray. First of all, I was convinced I knew how contactors work, because they’re basically just relays in terms of hookup. Second of all, I had learned the hard way back on Veronica’s EEPROM circuit that sometimes electronic parts are just dead, even when it seems super unlikely. All this added up to me convincing myself that the contactor had gone bad. All the evidence I had seemed to point in that direction, and I let myself fall into a mental trap about it. I was so sure that I think I even tweeted about it.
Given all this, I dropped another $50 at McMaster-Carr and ordered a replacement. The replacement came in and…. wait for it… behaved the same way. Well, poop.
If you’re experienced with AC machinery or industrial process components, you’re screaming at your web browser right now because you know what I did wrong. Contactors are wired like DC electronics relays, sure. But they do not behave like them! Contactors need a load on their output to function. The contactor does not turn on and off with nothing but a voltmeter hanging off the output. If I understand correctly, this is because the contactor is waiting for a zero-crossing in the AC frequency to make the on/off transition (to prevent arcing), and without a load passing current, it never sees one. Feel free to correct me in the comments if this incorrect. What I don’t know about AC would fill a warehouse, so I’m just guessing here about why a load is required.
However, I still wasn’t emotionally prepared to sacrifice my heating element on this altar of my own ignorance, so I did one more test with a real AC load. I grabbed the closest thing handy, which was…

… my iPhone charger. I spliced this into my test circuit, and low and behold the contactor worked perfectly. Interestingly, the contactor did stutter on/off a bit. I suspect this is due to the iPhone charger being a switching power supply.
After confirming everything was working, I swallowed my pride, hooked up the real heating element, and tested again. Everything worked perfectly, of course. I had the wiring right all along, and none of this drama was necessary. I placed my fancy extra contactor on the junk pile. I’m sure it will be used for something someday, and I got a $50 education in AC machinery control.
With the electrical sorted out, there was nothing left but to fill the boiler with distilled water, plug it in, and stand back. I timed the progress from cold, for future reference:
• 7 mins: Boiler too hot to touch
• 10 mins: Making noises like a tea kettle
• 13 mins: Water boiling(?) noises
• 20 mins: Pressure gauge starting to read
• 22 mins: Gauge reading 25psi
• 28 mins: Gauge reading 50psi
I can’t overstate how exciting it was to see the pressure gauge read for the first time. Seeing this crazy thing I made making actual steam pressure under its own power was insanely great.

This was VERY EXCITING. The boiler was actually making real steam pressure under its own power.
Now, that was exciting, but nothing compared to what is about to happen. You see, this first steam test had a dual purpose. In addition to making steam, I needed to test the safety valve. The top of the boiler has a blow-off valve set to 60psi (10 psi above normal working pressure) and it’s crucial to know that this valve works correctly before trusting the boiler. Not only does a blow-off valve release pressure, but it has to release a sufficient volume of steam to get down to safe levels quickly, and stay ahead of the pressure that is still building. This is a large volume of steam to be released in a short amount of time. I was…. unprepared for this.
I could hear a seeping sound start to come from the safety valve as the boiler got close to 60 psi, so I started filming to capture the moment. I thought the seeping sound was the valve doing its thing. Turns out that was the mountain lion growling at you just before it rips your throat out. Watch and see. Headphone wearers, turn down your volume.
I was completely unprepared for how much steam was released, and the force with which it comes out. Everything in a six foot area was completely soaked, I dropped the camera, and it took me some time to gather myself back up. The good news is, the blow-off valve worked perfectly! All in all, it was a great success and I learned more respect for 60psi of live steam.
With the boiler up to steam, I can test the globe valve that I’m using as a throttle.
Shazam! That’s a very nice blast of hot steam at 50psi. There’s a lot more water there than I’d like, and I believe this is because the boiler is overfull. I have a lot to learn about boiler operation, and I need to get to know the quirks of this boiler in particular.
Now that we can make steam, there’s just one more thing we need to run a real engine. We need a steam pipe to connect the engine to the throttle valve. Rather than relying on hydraulic sealant for these connections, I decided to try pushing my skills and see if I could make proper self-sealing flare fittings.
A flare fitting has three parts- a male cone, a female cone (or seat), and a captive nut which holds those tightly together. The actual sealing is done by the cone surfaces being precisely machined and seating together perfectly.
To make sure I understood what I was doing, I modeled the whole fitting in Fusion 360 first.
Looks easy enough. To the lathe!

First up is the cone. This is sized to slip over 1/4″ copper pipe, and the end is tapered to 37° using the compound-feed method. I chose 37° because that’s what JIC connectors use, and smart people probably figured out a reason for that.

The narrow portion was made by plunging a wide parting tool.
Next comes a great trick that I adapted from a suggestion from a friend on Instagram. Thanks, Rob! The idea is that, after you cut the flare for the cone, don’t touch the compound. Instead, put a boring bar on the toolbit side of the tool post, and run the lathe backwards. Because you haven’t touched the compound, the angle of the mating surfaces is guaranteed to be perfect (not counting spring in the boring bar, chatter, or other incidental artifacts).

A boring bar can juuust sneak in there and cut the flare seat from the back. Don’t forget to reverse the lathe for this!
With this trick, our odds of success for this fitting sealing properly are pretty high.

Looks great! Will it seal?

The flare seat was then flipped around to have the other threads cut. Copper soft jaws protect the finished surfaces. Note that we’ve flipped the part in a three-jaw chuck, which is a concentricity no-no, but it doesn’t matter for a simple plumbing fitting.
All seemed to be going well, until I came to make the clamping nut. I had modeled everything in Fusion 360 ahead of time, so it should have been perfect, right? Well, I didn’t use the “modeled threads” option in Fusion, so I didn’t see that the wall thickness of the nut was too thin for the depth of threads inside. I tweaked all the dimensions a bit, and made the three parts again.

Up top is my first attempt, which failed when I got to the nut. The dimensions were all tweaked to yield the bottom set, which worked really well.
The engine I’m going to test with is the first wobbler I ever made, so I needed the other end of the steam pipe to fit the 10-32 inlet on that engine.

This very weird adapter mates the small 10-32 inlet on the wobbler to the 1/4″ flare fitting on the steam pipe.
Through the magic of television, we instantly do all that again.

Here are the final two sets of fittings. They look great, but I still have no idea if they will seal.
The cones in a flare fitting are soldered to the pipe, and the nuts are held captive behind them on the pipe. It’s time for some silver soldering.

This pipe is from the junk pile, so it needed some cleaning before soldering. The cones were a perfect fit, and I even remembered to slide the nuts on before soldering.
Compared to silver soldering the boiler itself, connectors like this are incredibly, incredibly easy. A few seconds with the Map/Pro torch, and it’s done.

The Map/Pro torch burns dirty, so it makes a sooty mess of our pipe, but it’s very easy.
A little cleanup with Scotch Brite, and our pipe is ready for service.

Looking good! Making your own plumbing fittings from scratch is actually very satisfying.
Okay, let’s get it hooked up!

A little Loctite 545 was used on the adapter in the engine, since that’s just a plain straight thread and isn’t likely to seal well.
The good news is, both fittings sealed perfectly. I was very pleasantly surprised that neither fitting needed any sealant, and with minimal tightening pressure they sealed 50psi flawlessly on the first try. I’ll definitely be making my own fittings again in the future!
Now I know what you’re thinking. Show us the engine running on steam. Luckily, I have some great video of it, but that’s reserved for Patrons. If you’re a Patron, you already have this video in your in-box. There’s also a little tour of where the boiler is now, and the work that will coming on it.
If you’re not a Patron, this is a great time to sign up because there will be a lot more videos and other perks coming your way! Want some Blondihacks stickers? You can get them over on Patreon. They’re pretty sweet, if I do say so myself.
There’s still a lot more to do on this boiler, including finalizing the electrical work and building the base, so stay tuned for all that!